British Airways Flight 5390

British Airways Flight 5390

A British Airways BAC 1-11 similar to the aircraft involved in the incident.
Incident summary
Date 10 June 1990
Summary Explosive decompression due to faulty maintenance
Site Didcot, Oxfordshire, England
Passengers 81
Crew 6
Injuries (non-fatal) 2
Survivors 87 (all)
Aircraft type BAC 1–11 528FL
Aircraft name County of South Glamorgan
Operator British Airways
Registration G-BJRT
Flight origin Birmingham Airport
Destination Málaga Airport

British Airways Flight 5390 was a scheduled passenger flight operated by British Airways between Birmingham Airport in England and Málaga Airport in Spain. On 10 June 1990 an improperly installed panel of the windscreen failed, blowing the plane's captain, Tim Lancaster, halfway out of the aircraft. With Lancaster's body firmly pressed against the window frame for over twenty minutes, the first officer managed to perform an emergency landing at Southampton Airport with no loss of life.

Incident

The aircraft, County of South Glamorgan, captained by 42-year-old Tim Lancaster, who had logged 11,050 flight hours, and co-piloted by 39-year-old Alastair Atchison, who had logged 7,500 flight hours,[1] was a BAC One-Eleven Series 528FL registered as G-BJRT.[2] It took off at 07:20 local time, with 81 passengers, four cabin crew and two flight crew. Co-pilot Atchison handled a routine take-off, and relinquished control to Lancaster as the plane established itself in its climb. Both pilots subsequently released their shoulder harnesses, while Lancaster loosened his lap belt as well.

At 07:33, the cabin crew had begun to prepare for meal service. The plane had climbed to 17,400 feet (5,300 m) over Didcot, Oxfordshire. Suddenly, there was a loud bang, and the fuselage quickly filled with condensation. The left windscreen, on the captain's side of the cockpit, had separated from the forward fuselage. Lancaster was propelled out of his seat by the rushing air from the rapid decompression and forced head first out of the cockpit, his knees snagging onto the flight controls. This left him with his whole upper torso out of the aircraft, and only his legs inside. The door to the flight deck was blown out onto the radio and navigation console, blocking the throttle control, causing the aircraft to continue gaining speed as it descended, while papers and other debris in the passenger cabin began blowing towards the cockpit. He hung out the window for a moment or more, when at the time, flight attendant Nigel Ogden saw the situation in the cockpit, and quickly rushed to latch his hands onto the captain's belt. Susan Price and another flight attendant began to reassure passengers, secure loose objects, and organise emergency positions. Meanwhile, Lancaster was being battered and frozen in the 345 mph wind,[3] and was losing consciousness due to the thin air, with the outside air temperature around -17 C / 1.4 F, not including the chill from the incredible wind.

Atchison began a very rapid emergency descent to reach an altitude with oxygen because the plane was not equipped to provide it for all persons on board. Then he re-engaged the temporarily disabled autopilot, and broadcast a distress call. Due to rushing air on the flight deck, he was unable to hear the response from air traffic control. The difficulty in establishing two-way communication led to a delay in British Airways being informed of the emergency and consequently a delay in the implementation of the British Airways Emergency Procedure Information Centre plan.

Ogden, still latched onto Lancaster, had begun to suffer from frostbite, bruising and exhaustion. He was relieved by the remaining two flight attendants. By this time Lancaster had already shifted an additional six to eight inches out the window. From the flight deck, the flight and cabin crew were able to view his head and torso through the left direct vision window. Lancaster's face was continuously hitting the direct vision window; when cabin crew saw this and noticed that Lancaster's eyes were opened but not blinking despite the force against the window, they assumed that Lancaster was dead. Atchison ordered the cabin crew to not release Lancaster's body despite the assumption of his death because he knew that releasing the body might cause it to fly into the left engine and cause an engine fire or failure which would cause further problems for Atchison in an already highly stressful environment.

Eventually Atchison was able to hear the clearance from air traffic control to land at Southampton, while the flight attendants managed in extreme conditions to free Lancaster's ankles from the flight controls and hold on to him for the remainder of the flight. By 07:55 the aircraft had landed safely on Runway 02 at Southampton. Passengers immediately disembarked from the front and rear stairs, and emergency crews retrieved Lancaster.

Injuries

Much to everyone's surprise, Lancaster was found to be alive, and was taken to Southampton General Hospital, where he was found to be suffering from frostbite, bruising and shock, and fractures to his right arm, left thumb and right wrist. Flight attendant Nigel Ogden suffered a dislocated shoulder, frostbitten face and some frostbite damage to his left eye. Everyone else left the aircraft unhurt.[4]

Less than five months after the accident Lancaster was working again. He later retired from British Airways when he reached the company's mandatory retirement age of 55 at the time. In 2005 Lancaster was reported flying for easyJet.[4]

Investigation

Accident investigators found that a replacement windscreen had been installed 27 hours before the flight, and that the procedure had been approved by the shift maintenance manager. However, 84 of the 90 windscreen retention bolts were 0.026 inches (0.66 mm) too small in diameter, while the remaining six were 0.1 inches (2.5 mm) too short. The investigation revealed that the previous windscreen had been fitted with incorrect bolts, which had been replaced on a "like for like" basis by the shift maintenance manager without reference to the maintenance documentation, in order to save time as the plane was due to take off soon and there was a tight schedule.[5] The air pressure difference between the cabin and the outside during the flight proved to be too much, leading to the failure of the windscreen. The incident also brought to attention a design flaw in the aircraft of the windscreen being secured from the outside of the aircraft, putting a greater pressure on the bolts than if they were secured from the inside.

The windscreen was recovered in a field outside Didcot, Oxfordshire by officers from Thames Valley Police. With earlier officers having not searched for or collected the bolts from the site, PC Tony Nash returned to the site and located a number of the windscreen bolts that assisted in determining the cause of the incident.

Investigators found the British Airways Birmingham Airport shift maintenance manager responsible for installing the incorrect bolts during the windscreen replacement and for failing to follow official British Airways policies. They also found fault with British Airways' policies, which should have required testing or verification by another individual for this critical task. Finally, investigators found the local Birmingham Airport management responsible for not directly monitoring the shift maintenance manager's working practices.

Safety recommendations

Investigators made eight safety recommendations in the final accident report:

British Airways

Civil Aviation Authority

Dramatic reconstructions

This incident was featured on the Discovery Channel Canada programme Mayday (National Geographic Air Crash Investigation in other parts of the world), called "Blowout",[6] which was retitled Ripped From The Cockpit: BA Flight of Terror when broadcast on Channel 5 in the UK.

Awards

First Officer Alastair Stuart Atchison and cabin crew members Susan Gibbins and Nigel Ogden were awarded the Queen's Commendation for Valuable Service in the Air (Although Ogden's name was erroneously missed from the published supplement).[7]

Atchison was awarded a 1992 Polaris Award for his ability and heroism.

Use of flight number

Flight number 5390 is now used for a British Airways codeshare route operated by Envoy Air, between Des Moines, Iowa, and Chicago-O'Hare, Illinois, in the United States.[8]

See also

References

  1. http://www.aaib.gov.uk/cms_resources/1-1992%20G-BJRT%5B2%5D.pdf
  2. "GINFO Database". Civil Aviation Authority.
  3. "SPECIFICATIONS". bac1-11jet.co.uk. Retrieved 31 October 2015.
  4. 1 2 "This is your captain screaming (interview with Nigel Ogden)". The Sydney Morning Herald. 5 February 2005. Retrieved 21 April 2008.
  5. Official AAIB report, p.38
  6. Blow Out (2004) (Air Emergency: Season 2, Episode 1) at the Internet Movie Database
  7. The London Gazette: (Supplement) no. 52767. p. 27. 30 December 1991. Retrieved 18 May 2010.
  8. "British Airways (BA) #5390 Flight Tracker". FlightAware. Retrieved 30 January 2013.

External links

Coordinates: 51°36′21″N 1°14′27″W / 51.60583°N 1.24083°W / 51.60583; -1.24083

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